Minutes of the Tracker Technical Meeting
February 6, 2003
Action Items
1. Luca: check whether the MCMs work better if VDD is raised or the clock
frequency lowered.
2. Tom/Dave: see if the Kapton bias circuit
can be procured with a peel-off protective cover.
3. Dave: reverse VDD and Bias at the extreme
ends of the bias circuit and MCM.
4. Sandro: send encapsulated ladder test
results to Robert and Darren.
5. Nick: send the French composites
procedures to use as an example.
6. Darren: look into how we should track
inserts and other fasteners during flight fabrication.
7. Sandro: send a drawing of the desired
alignment hole pattern for the bias circuits.
8. Dave: move copper and gold away from the
trim line on the bias circuits.
9. Tom: get the thick tungsten order going.
10. Nick: resolve Dave’s question about the
use of a 4V tantalum capacitor.
Sandro reported that G&A is still working
on the system to do wire bonding of MCMs to ladders. Next Tuesday they will wire bond from the MCM to the bias
circuit. Then they will glue ladders on
and wire bond to the ladders. This is
about a week behind schedule, but Sandro believes that there is still enough
time to catch up, as the actual work should go fast once underway.
Luca reported that the Pisa MCM test
procedure & results are on the Pisa web page under the EM tower link. They found all defects mentioned by UCSC
plus a few more. In particular, for MCM
75 the register read-back always gives errors.
Robert noted that UCSC raised VDD or lowered the clock frequency to
account for the poor timing margin in the existing system (should be fixed in
the chips now in fab). Pisa will check
whether the new errors are due to the timing problem.
Sandro reported that Plyform is gluing
tungsten & Kapton on the remaining panels.
The Kapton alignment is good.
They tested by vibration 4 trays.
Three of them had some known defects during assembly (they were some of
the first panels built). The defects
can be readily observed in the shake test, from a lowering of the resonant
frequency. Nevertheless, there were no
changes in frequency from random vibe test, comparing before and after the
test. There also was no damage. The work confirmed that they can do 4 tray
tests per day, as required. The
fundamental frequency of the good tray was above 850Hz. Silicon will lower this to about 700Hz. The Q was about 47. For one of the trays with gluing problems
the frequency was about 560Hz. The tray
destined to be used for qualification testing with live ladders and electronics
was above 900Hz.
Next week they will try out the holographic
system on these trays. Sandro said that
they will buy this Frascati holographic system for use either at Pisa or
Plyform.
Sandro said that the trimming process for the
face sheets and Kapton contaminates the Kapton surface. He would like to buy Kapton foil with a protective
cover that can be peeled off at the last moment. SLAC will look into this.
Sandro said that the edge bias bond pad
(AVDDA) is not in a good position for the bias bond to the SSD. (This will be solved by interchanging AVDDA
and BIAS at the two extreme ends of the bias circuit and the MCM.)
G&A ladder status. 80 encapsulated ladders are under test. However, the Perugia operator became ill and
stopped the tests. Another group of
ladders will be ready next week, and the Roma-2 group will be doing the testing. Sandro does not have the details from the
first tests but will send more information tomorrow to Robert and to Darren.
MIPOT status: the Nusil encapsulant finally
is in Pisa. Sandro will go to Mipot the
week after next with all materials and the inox storage boxes. He will then discuss ladder production startup
with Mipot. He will propose that they
build 10 ladders, wait for review, and then do 90 more ladders.
Sandro is translating the Plyform procedures
from Italian into English. Tom will
leave 19th February to travel to Italy, arriving in Milan February 20 shortly
after lunch. He will be at Plyform that
afternoon and Friday and Monday. He
would like to visit Pisa Tuesday, and he will leave February 27.
There was a discussion of the schedule for a PRR
of the tray panel production. We will
shoot for the week of 10 or the 17 of March.
Tom will close this plan when over there. Nick will send the French composite procedures as a
guideline. Tom will forward them to
Sandro.
Aluminum handling and storage boxes are ready
for the 4 live trays. They will be shipped
with trays to SLAC in wood boxes with plenty of foam.
Tom reported that the order has been placed
for cores, which will arrive by the end of the month and then will ship to
Italy. The carbon-carbon is still at
SLAC. Tom is trying to figure out how
to mark the bars with serial numbers. A
SLAC technician is being found to do the work.
Responding to Robert’s questions, Sandro
explained that the inner face of the CC closeout is coated at the beginning,
prior to panel assembly. The outer face
is coated at the very end. Sandro is
interested in using black paint instead of the resin (the same black paint that
we intend to use to increase the tower-module emissivity).
Sandro said that inserts are included in the
Plyform order, so it will be their responsibility to procure them. Robert asked how are the inserts tracked
(material, by lot, etc). Darren will
look into this.
Bias circuits: Sandro said that we need to
change the position of reference holes to make them asymmetric, so that they
cannot be put on backwards. Sandro will
send a drawing. Also, the existing
circuit has one hole out of place, apparently due to an error at Parlex. Tom said that SLAC will get an inspection
procedure in place to make sure that our flight procurements match the drawings. Sandro also said that the copper/gold ring
all around the bias circuit must stay 2 mm outside the cut so it doesn't
interfere with trimming.
Thin tungsten: Sandro reported that an order
has been placed for 10% extra material.
He is starting to prepare the order for cutting, which will be done by
water jet. The blank sheets should arrive
at the end of March. The cutting can be
done in 2 or 3 weeks.
Thick tungsten: Tome said that he has a discussion
going with the project office to get help with ordering. Tom will talk to Debbie & Shannon about
getting these orders out. The lead
times are not bad for material but can be an issue for the double disk
grinding.
Electronics parts: polyfuses, PWB, HV caps,
SMT parts all need to be ordered.
Robert is working on closing out issues with the polyfuse procurement
specification, but the order should go out now, anyway, as the requirements on
the manufacturer have been settled (some issues remain regarding testing by a
third party after delivery). The HV
capacitor specification is released, so those are being purchased. There is one unresolved voltage rating issue
with a tantalum capacitor (can we use a 4V part with a 2.5V supply?).
Erik reported that Hytec is still working on the
model. They modified the closeout
design slightly to relieve problems with stress concentrations in the corners. The closeouts now are nearly all M55J, with
just small layer of carbon-carbon for machining the outer surface. (Thermal conductivity through the bulk is no
longer a big issue for these parts, because of the heat straps.) The corner bracket has a taper to relieve
peel stress. The carbon-carbon now
extends just to the end of the taper.
Most of titanium bonds directly to M55J. Tom said that he is thinking that the EM closeouts should be
fabricated at COI. He would like to do
the same for the flight hardware to be consistent. There is a question about when to install the midspan inserts for
flexures. It may be best to wait until
after panel assembly, so that the flexure alignment and insert installation can
be done together. In any case, the sidewall
inserts can go in earlier, prior to panel assembly. Tom will review this when in Italy. Erik suggested that we don't necessarily need shoulder screws for
the sidewall flexures, since they will be bonded to the closeout, so the
inserts could be put in earlier without worrying about alignment tolerance. Tom will take drawings to Italy and go over
the bottom tray assembly and tower assembly with Sandro. Erik noted that the design modifications
should not change the tray panel assembly procedure in Italy.
The M55J will get no machining except for
hole drilling and edge cuts. There will
be no cutting into the fibers. Erik
said that they may lay it up heavy with resin on the top so that they can take
a skim cut through the resin on the top side.
The smooth flat mold side is on the inside surface.
Hytec is in the middle of the analysis on the
load fixture. Franz is doing this,
while Steve is working on the bottom tray analysis. Erik wants to get the load fixture components out to the machine shop
quickly.
Tom said that so far there are no results on
the acoustic analysis except hearsay that the numbers are coming in lower. It should be completed by the end of the week.
Erik said that the thermal strap design has
been modeled. There are some stress
issues in the copper. They may simply
be immediately relieved in practice by plastic flow of the material. Either a stronger allow is needed, or else
the material flow must be studied.
Tom said that there is a tower ICD
modification. We will go to a 30C
operational limit. This gives 3 degrees
more margin for us and 2 for the Grid.
The mechanical ICD needs a drawing from
Martin for release.
Robert discussed the peer review
preparations. We need some kind of
design report, but keep it simple. It
does need to cover well the bottom tray stuff. Erik will look at the old report and see what needs updated. We also need to document test results as
they are available.